Delta Air Lines Flight 1288
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Delta Air Lines Flight 1288 was a regularly scheduled flight from
Pensacola, Florida Pensacola () is the westernmost city in the Florida Panhandle, and the county seat and only incorporated city of Escambia County, Florida, United States. As of the 2020 United States census, the population was 54,312. Pensacola is the principal c ...
, to
Atlanta, Georgia Atlanta ( ) is the capital city, capital and List of municipalities in Georgia (U.S. state), most populous city of the U.S. state of Georgia (U.S. state), Georgia. It is the county seat, seat of Fulton County, Georgia, Fulton County, the mos ...
. On July 6, 1996, the aircraft serving the flight, a McDonnell Douglas MD-88, was on takeoff roll from Runway 17 at Pensacola when it experienced an uncontained, catastrophic
turbine engine failure A turbine engine failure occurs when a turbine engine unexpectedly stops producing power due to a malfunction other than fuel exhaustion. It often applies for aircraft, but other turbine engines can fail, like ground-based turbines used in power ...
that caused debris from the front compressor hub of the left engine to penetrate the left aft fuselage. The cause of the engine failure was judged to have been a fault in the manufacture of the fan, and failure of the airline to spot the resulting crack in the blade. The impact left two passengers dead and two severely injured; the two dead were a mother and son. The pilot aborted takeoff and the airplane stopped on the runway. Three other passengers sustained minor injuries during the
emergency evacuation Emergency evacuation is the urgent immediate egress or escape of people away from an area that contains an imminent threat, an ongoing threat or a hazard to lives or property. Examples range from the small-scale evacuation of a building due t ...
. Most of the passengers were traveling on vacation.


Aircraft and crew

The aircraft involved was an 8-year-old McDonnell Douglas MD-88 registered as It was built in April 1988 and delivered to Delta in November the same year. The aircraft was equipped with two Pratt & Whitney JT8D-219 turbofan engines. It had 22,031 flight hours and 18,826 take off and landing cycles at the time of the accident. The 40-year-old captain had been with Delta Air Lines since 1979, having previously flown for a commuter airline. He had 12,000 flight hours, including 2,300 hours on the MD-88. The 37-year-old first officer had been with Delta since 1990, having logged 6,500 flight hours, with 500 on them on the MD-88. The first officer had previously been a United States Air Force pilot.


Pre-flight inspection

During the
pre-flight inspection In aviation, an outside check or walk around is the air crew inspecting certain elements of an aircraft prior to boarding for security, safety, and operational reasons. The pilot primarily inspects outside parts of the aircraft they will stee ...
, the first officer noted a few drops of oil coming from the "bullet" or tip of the number one (left) engine, although it was said to be "not that serious". The first officer also noticed a couple of missing rivets on the left wing. The pilot told
National Transportation Safety Board The National Transportation Safety Board (NTSB) is an independent U.S. government investigative agency responsible for civil transportation accident investigation. In this role, the NTSB investigates and reports on aviation accidents and inci ...
(NTSB) investigators that both problems were observed as non-threatening and that the aircraft was airworthy; therefore, maintenance was not informed.


Takeoff and accident

At 2:23 pm CDT, Delta flight 1288 was cleared for takeoff on Runway 17. As the first officer was advancing the throttles and reaching an airspeed of , the cockpit lost lighting and instrumentation. The rear cabin passengers and flight crew heard a very loud bang and experienced a blast-like sensation. The pilot then ended takeoff by bringing the throttle to idle and engaging the brake, which brought the aircraft to an eventual stop without use of reversers or spoilers. Once the aircraft stopped, the first officer attempted to contact the tower; however, he was unable due to the cockpit's lack of power. The flight crew then activated emergency power, contacted Pensacola tower, and declared an emergency. The cockpit's jump-seat passenger, an off-duty Delta
Boeing 767 The Boeing 767 is an American wide-body aircraft developed and manufactured by Boeing Commercial Airplanes. The aircraft was launched as the 7X7 program on July 14, 1978, the prototype first flew on September 26, 1981, and it was certified o ...
pilot deadheading with the fellow cockpit crew members, went to inspect the rear of the aircraft. When the first officer saw the over-wing exits open and about half of the passengers missing along with hearing engine noise, he returned to the cockpit and advised the captain to shut down the engines. At 2:27 pm CDT the pilot requested emergency medical assistance due to the jump-seat passenger's report of a large hole in the fuselage, engine debris throughout the cabin, and injured passengers. He then reported there was no evidence of smoke or fire in the cabin, and that the rear cabin door had been opened and the emergency slide was inflated. The flight attendant who initiated the evacuation through that door told the NTSB that she saw fire on the left engine and therefore abandoned evacuation through that door and directed passengers forward. She reported that there were many injuries and possibly two dead, and that therefore she began to evacuate the plane until she was stopped by the first officer. Due to the damage to and danger at the rear of the aircraft, the air stairs built into the MD-88 were found unsuitable to use. The captain then requested portable air stairs to facilitate the disembarkation of passengers, which arrived 25 minutes later.


Injuries and deaths

Two passengers suffered fatal injuries. Five more passengers were injured; one of them was noted to be in serious condition.


NTSB investigation

After a total investigation, the NTSB determined the most probable cause of the accident was a fracture in the left engine's front compressor fan hub, which resulted from failure of the airline's fluorescent penetrant inspection process to detect a potentially dangerous crack in the fan which originated from the engine's initial manufacture. The NTSB also attributed the accident to the failure of Delta's maintenance team to discover the problem.


Aftermath

As of April 2018, the FAA reports the aircraft involved in the accident was repaired and returned to service with Delta under the same registration The aircraft was withdrawn from use by Delta on August 10, 2018.


See also

*
Delta Air Lines Flight 1086 Delta Air Lines Flight 1086 was a scheduled Delta Air Lines domestic passenger flight between Atlanta and New York's LaGuardia Airport. On March 5, 2015, the McDonnell Douglas MD-88 aircraft veered off the runway shortly after landing at LaG ...
– An accident that happened in 2015, involving another McDonnell Douglas MD-88, without fatalities *
Southwest Airlines Flight 1380 Southwest Airlines Flight 1380 was a Boeing 737-7H4 that experienced a contained engine failure in the left CFM56-7B engine after departing from New York–LaGuardia Airport en route to Dallas Love Field on April 17, 2018. The engine cow ...
– A similar accident that happened in 2018, with one fatality *
Southwest Airlines Flight 3472 Southwest Airlines Flight 3472 was a regularly scheduled passenger flight operating from New Orleans International Airport in New Orleans, Louisiana to Orlando International Airport in Orlando, Florida. On August 27, 2016, the Boeing 737-7H4, w ...
– A similar accident that happened in 2016, without fatalities *
British Airtours Flight 28M British Airtours Flight 28M (also known as Flight 328) was an international passenger flight which caught fire before takeoff at Manchester Airport, England on 22 August 1985 with the loss of 55 lives. It was en route to Corfu International A ...
, a
Boeing 737 The Boeing 737 is a narrow-body aircraft produced by Boeing at its Renton Factory in Washington. Developed to supplement the Boeing 727 on short and thin routes, the twinjet retains the 707 fuselage width and six abreast seating with two u ...
that abandoned their takeoff from
Manchester Airport Manchester Airport is an international airport in Ringway, Manchester, England, south-west of Manchester city centre. In 2019, it was the third busiest airport in the United Kingdom in terms of passenger numbers and the busiest of those ...
after a
combustor A combustor is a component or area of a gas turbine, ramjet, or scramjet engine where combustion takes place. It is also known as a burner, combustion chamber or flame holder. In a gas turbine engine, the ''combustor'' or combustion chamber is f ...
exploded in the left engine, killing 55.


References


External links


NTSB investigation docket
{{Delta Air Lines Airliner accidents and incidents in Florida Aviation accidents and incidents in 1996
1288 Year 1288 ( MCCLXXXVIII) was a leap year starting on Thursday (link will display the full calendar) of the Julian calendar. Events By place Europe * June 5 – Battle of Worringen: Dutch forces under Duke John I (the Victorious) ...
Accidents and incidents involving the McDonnell Douglas MD-88 Escambia County, Florida 1996 in Florida Aviation accidents and incidents in the United States in 1996 July 1996 events in the United States Airliner accidents and incidents involving uncontained engine failure