Flight and aircraft
The aircraft, named ''Sunbreeze'' (registration EC-HFP; constructor's number 53148), had been manufactured in late 1993 and was acquired by Spanair in July 1999. There were 166 passengers and six crew members on board, including the 39-year-old captain, Antonio Garcia Luna, and the 31-year-old first officer, Francisco Javier Mulet.Prior to the accident
Fifty-nine minutes before the flight's second attempted take-off, the pilots had abandoned a departure because of excessive temperatures in the ram air temperature (RAT) probe. The aircraft was taken to a parking area where maintenance workers de-activated the RAT probe's heater. The aircraft was permitted to fly with an inoperable RAT probe heater because icing was not expected during the flight. Another takeoff was then attempted, during which the accident occurred.Accident
The accident occurred during the second attempt, at 14:24 local time, due to the pilot's failure to deploy the flaps and slats as required for takeoff. Without the use of these "high-lift" devices, the wings could not generate enough lift to keep the aircraft airborne. The MD-80 has a warning system (the take-off warning system or TOWS) that should have alerted the pilots that the aircraft was not correctly configured for take-off. However, the warning did not sound, and the pilots continued with the attempt. As the aircraft took off, itCrash sequence
Just 3 seconds after lift off the aircraft started shaking and banking both sides. The stall warning horn activated as well as the synthetic voice. The first officer called in interrogative tone an engine failure and reduced power on both engines, specially on the right one, increasing the bank angle on the right to 32 degrees, immediatelly after this, he pushed the engines to their full power and the pitch increased to 18 degrees. The aircraft impacted the ground just right of the runway with its tail section first, then its right wingtip and its right engine. The aircraft travelled on the ground, causing a few components to detach from the aircraft. The aircraft later lost contacted with ground when it jumped over an enbankment. The landing gears and the engines deatached from the aircraft and the plane continued sliding on the ground then coliding with another small enbankment. In this impact the tail was torn off, the cockpit collapsed into the passenger area and the fuel leaked and ignited into a fireball. The aircraft engulfed in flames continued sliding on the ground until it reached De la Vega stream and collided with the riverbank. The fuselage was highly fragmented by the crash and had been damaged by the fire. The front third of the fuselage was on the stream bed, while the rear two-thirds were on the north side of the stream. The wings and the rear two-thirds of the fuselage were engulfed and destroyed by fire.Victims
Of the 172 on board, 146 perished in the crash or immediately after in the fire, including both pilots. Of the twenty-six passengers and crew rescued alive from the crash site, six died before arriving at hospital, and two more died in hospital, bringing the total number of fatalities to 154. Most of the deceased and 16 of the survivors were Spanish nationals. Nineteen of the deceased and two survivors were of other nationalities. Among the victims, there were 15 victims of other nationalities including Germany, France, Mauritania, Turkey, Bulgaria, Gambia, Italy, Indonesia, and Brazil. The crash threw some of the survivors clear of the wreckage and into a stream, lessening the severity of their burns. A 30-year-old woman with British and Spanish dual citizenship survived with a punctured lung and broken left arm but no burns, as she was thrown from row 6, still attached to her seat, into the stream.Investigation
Summary
The accident was investigated by the Civil Aviation Accident and Incident Investigation Commission (CIAIAC). Representatives from the USTheories
Fire or explosion
Some early eye-witness accounts suggested that the aircraft suffered an engine fire or explosion before crashing, but the Spanish airport authority AENA released a video showing that the engines neither exploded nor caught fire during take-off. Manuel Bautista, Director General of Spain's civil aviation authority, went as far as to state: "The engine is not the cause of the accident", surmising that a chain of events combining together was more likely than a single cause.Temperature sensor
There was considerable interest in the faulty air temperature probe (the RAT sensor,The aircraft'sThrust reverser
Pictures of the wreckage showed one of the thrust reversers in the deployed position, and an early theory constructed in the media was that the thrust reverser of the No. 2 (right side) engine activated during the climb causing the aircraft to yaw suddenly to the right. This theory fell apart for three reasons: firstly, aircraft engineer Alberto Garcia pointed out that the MD-82 has tail-mounted engines positioned close to each other and to the aircraft's longitudinal axis, so that any yaw from asymmetric thrust would be small. Secondly, examination of the aircraft's maintenance logs showed that the thrust reverser on the right-side engine had been deactivated pending repair. It had been wired shut, and tape placed over the cockpit control to alert the crew. The MD-82 is permitted to fly with just one operable thrust reverser. Thirdly, the engine which had been pictured was the left engine, not the right one. The investigation concluded that the position of its thrust reverser was a result of the accident, not a cause of it.Flaps and slats
'' El Mundo'' reported that the CVR showed that the pilot had said "Flaps OK, Slats OK" to the co-pilot. The article confirmed that the flaps had not been extended and that the alarm for that condition had not sounded. The final report concluded that the failure to deploy flaps was the cause of the accident. The maintenance logbook of the aircraft has comments, two days before the crash, for an "autoslats failure" visual alarm occurring on slats extension; however autoslats are not used on takeoff, and it cannot be inferred that the slats system had a defect.Flight mode
In an article published on 7 September, ''El Mundo'' suggested that during the flight preparation and takeoff attempts, the aircraft had some of its systems in flight mode rather than ground mode. Investigators noted that one particular ground-sensing relay (relay R2-5) was responsible for de-energizing the RAT probe heater when on the ground, and for inhibiting TOWS when in the air. They theorised that a fault in this relay could explain both the overheating of the probe and why the flaps and slats alarm had not sounded. When the R2-5 relay was recovered from the wreckage it was subjected to detailed examination. Two stuck contacts within the relay were identified, which would explain the overheating both on the day of the accident and the intermittent incidents recorded over the previous few days. That fault, however, would not have affected the operation of the TOWS system, and no fault was found that would have affected TOWS. James W. Hudspeth, an investigator of a previous near accident (an MD-83, starting from Lanzarote) that was superficially similar, pointed out that the fuse of the so-called "left ground control relay" at position K-33 of the control panel might have been the actual culprit in the erroneous flight mode: Hudspeth found out during a 2-week investigation at Lanzarote that it is customary in normal maintenance routine to temporarily remove this circuit-breaker to engage flight mode, but the circuit-breaker is afterwards sometimes not replaced correctly. Because of the frequent handling of this circuit-breaker, it is also not easy to visually check that it is set properly. The CIAIAC team on the case of JK 5022 discounted this possibility because if the circuit-breaker had been left open it would also have affected the operation of theMalware
Spanish daily ''Final report
The CIAIAC published its final report into the accident on 26 July 2011. It determined that the cause of the accident was: * The crew lost control of the aircraft as a result of a stall immediately after takeoff, which was caused by an incorrect configuration for take-off (i.e. not deploying the flaps and slats, following a series of errors and omissions), coupled with the absence of any warning of the incorrect configuration. * The crew did not recognise the indications of stall, and did not correct the situation after takeoff, and – by momentarily retarding the engine power and increasing the pitch angle – brought the aircraft closer to a stall condition. * The crew did not detect the configuration error because they did not properly use the checklists to select and check the position of the flaps and slats during flight preparation, specifically: ** they failed to select the flaps/slats lever during the corresponding step in the "After Start" checklist; ** they did not cross-check the position of the lever and the state of the flaps/slats indicator lights during the "After Start" checklist; ** they omitted the flaps/slats check on the 'Take Off Briefing' (taxi) checklist; ** no visual inspection of the flaps and slats was carried out in execution of the "Final Items" step of the "Take Off Imminent" checklist. The CIAIAC determined the following contributory factors: * The absence of any warning of the incorrect take-off configuration because the TOWS did not work. It was not possible to determine conclusively why the TOWS system did not work. * Inadequate crew resource management (CRM), which did not prevent the deviation from procedures and omissions in flight preparation.In media
* "Deadly Delay", a 2016 episode of '' Mayday'', covered the investigation into the crash. * "Stalling on Takeoff", episode 33 of the ''Black Box Down'' podcast fromSee also
*Notes
References
External links